2024-11-24 - Fixing a Sony SLV-E9 VCR ------------------------------------- A while ago, I got a Sony SLV-E9 VCR with various problems in the mechanism[0]. Most of the repairs are explained much better in [1] by 12voltvids (that video is about a different VCR, but the mechanism is the same). I'll still try to give a general overview of the repairs I did. One general note before I forget it: If a VCR behaves weirdly when the cover is off, it might be because the infrared sensors are confused. This generally doesn't matter with LED lighting, but sunlight and incandescent lamps both cause issues. Power Supply ------------ WARNING: Fixing power supplies is dangerous, please don't kill yourself. Read up on safely discharging power supply capacitors before attempting any repairs. The top cover is held on by four screws on the two sides, but they were already missing when I got the VCR. When those are unscrewed, the cover can be removed[2]. I decided to look at the power supply before even trying to turn the VCR on. There is a small plastic cover held on by clips that has to be removed before removing the power supply[3]. There were definitely some bad capacitors in the power supply (very high ESR), but luckily none had leaked. I still ended up replacing all of them just in case. I'm not really a fan of replacing all capacitors when there isn't any reason to, but this VCR is pretty old and it's annoying to get into the power supply, so it was easier to just replace them all in one go. I won't go into any details here since most of the work was just replacing capacitors. The power supply board is soldered to the metal cage like in the SLV-815[4], but other than that, it isn't too complicated to replace the capacitors. Mechanism Disassembly --------------------- Most of the work I did was on the actual mechanism. To get to the mechanism, it is necessary to remove the front panel first, which is held on by plastic clips[5]. Note that there are two clips on the bottom of the VCR which sometimes require some prying with a flat-head screwdriver. The front panel is connected to the main board using a cable bundle. If needed, that can be unplugged from the main board so the front panel is out of the way. The loading mechanism can then be removed by unplugging the cables going to the motor and unscrewing four screws[6][7]. There is a hidden screw that needs to be removed before the mechanism can be taken out. The circuit board behind the front panel has a screw on the right and a connector on the left[8] (yes, I know that the picture was taken before the loading mechanism was removed). Once those are unscrewed/unplugged, the board can be flipped down (there are still some clips at the top that need to be pushed up for that to work). The hidden screw can then be accessed behind this board[9]. There is a circuit board attached to the bottom of the mechanism, which in turn is attached to the main board using two connectors that have to be opened to remove it[10] (note that that picture was taken at the end, after everything had been fixed). Other than that, there are a few screws on the borders of the mechanism that need to be removed. There was also one screw that I removed and then never found again[11], which is why it's missing in [10]. Note also that an automatic head cleaner is shown in [11]. I generally always remove those completely because they eventually get dirty and just end up making everything worse. I just clean the heads manually when I need to. WARNING: Do not use Q-Tips or anything similar to clean the heads. The usual recommendation is to just drench a piece of paper in isopropyl alcohol, lightly hold it against the head drum, and manually turn the drum while taking care not to move the paper up or down because that could break the heads. Please look at a proper guide before you attempt it yourself, this is just supposed to be a quick warning because many people have destroyed their heads with improper cleaning techniques. Once the mechanism has been removed, the circuit board on the bottom has to be unscrewed. I forgot to take any pictures of it, but it should be relatively self-explanatory. The main thing to watch out for is that the infrared sensors for sensing the tape ends are stuck through small holes in the mechanism, so take care not to snap them off while pulling the board away. Note: It is possible to remove the bottom cover of the VCR to get at the mechanism[35][36], but there are circuit boards in the way. Considering how annoying it was to get the mechanism out from the top side, it might still have been easier to just remove those circuit boards, though. Stuck Metal Arm --------------- The first problem with the mechanism was actually on the top side of the mechanism. A metal arm near the pinch roller was completely stuck[12]. This problem is also mentioned in [1], although in my case it was even more severe. I barely managed to open the nut holding it down. I then cleaned the shaft it was stuck on and the hole in the arm, and applied new grease. According to the video, you need to adjust the height once the VCR is in working condition by repeatedly going into rewind and fast-forward and screwing/unscrewing the nut until the tape doesn't curl on the top or bottom anymore. In my case, it seems I managed to screw the nut in to exactly the right height because I didn't have to adjust it at all later. Blue and White Gears -------------------- On the bottom side, the mechanism looks as shown in [13] (note that this picture was taken after repairing everything). I have also heard ([14]) that the edge of the capstan motor (on the bottom right) is magnetically coded, so you need to watch out that you don't damage it either with a magnet or with something hot (like a piece of hot solder). The main problem was that the infamous "blue gear" was completely cracked in half. I didn't take a picture of it, but [15] shows an intact one (actually, it's the one from the SLV-815 which also had a small crack in it already, but you can't see it in the picture). You can still get original blue gears in some places, but I decided to get a replacement from Van Eck[16]. In order to replace the blue gear, first the cam gear has to be removed (the large gear at the top left of [13]), for which the triangular metal piece holding it down has to be removed. Watch out that you don't lose any of the little metal rings that are used to hold it down. The metal arm that the blue gear is attached to can be removed completely by removing the metal ring fastening it to the tape guide on the other side[17]. I found it to be the easiest to also remove the white gear including its metal arm before removing the blue gear. The new blue gear can then be attached to the metal arm using the spring inside[18]. This usually isn't very difficult, but the replacement gear from Van Eck wasn't ideal because the middle part was way too thick for the hole in the metal arm, so I had to spend ages slowly grinding away at it until it fit properly. The blue and white gears need to be aligned properly, as shown in [19] (note that the sliding gear has also been removed in that picture - it should be possible to replace the blue gear without doing that, but I had to replace it anyways, as will be explained shortly). There is an arrow in the white gear that points at the smaller hole in the blue gear. On the original blue gear, there is another marking opposite the arrow[15], but that wasn't included in the replacement from Van Eck. There was another issue in this area of the mechanism that I only noticed later. Some plastic had broken off underneath the metal arm for the white gear[20], causing it to get stuck while loading a cassette. I cut out small parts from some scrap plastic I had, filed them down to the correct height, and stuck them on with 2-component epoxy[21]. It's not perfect, but I greased it properly and it seems to work fine so far. Talking about greasing, I've heard various opinions on grease. Many people swear by Super Lube (also called Synco Lube in Europe), although there are also different versions of that. I did actually get some Super Lube, but I don't really like it because it contains PTFE. Apparently lithium grease attacks plastic, so the gears should generally be greased with silicone grease, but some silicone grease is fairly sticky because it doesn't have PTFE or something similar to make it slippery (now that I think of it, I'm pretty sure I used some of that sticky silicone grease on the gears around the clutch assembly in the SLV-815, so maybe it would have worked if I had used a different type of grease). I eventually started just using the Super Lube since I had bought that already anyways, and I greased all the gears that originally had grease on them (but I left the gears that didn't have any grease on them, so I didn't make the same mistake as with the SLV-815). However, there are still two different types of Super Lube, one is the multi-purpose grease, and the other is silicone grease. I would assume that the silicone grease should be used for plastic gears, but many people seem to use the regular multi-purpose grease, so I'm a bit confused. Long story short, I have no idea what grease is best, and whatever you do, it will probably be wrong anyways. More Broken Gears ----------------- Anyways, there were two more broken gears in the mechanism. One was the gear between the worm gear and cam gear[22] (part number 3-736-015-01), the other one was the slide gear[23] (3-736-177-01). These proved to be much more difficult to find than the blue gear. After searching a lot online, I did manage to find sellers for both, but it ended up costing much more than the VCR was worth (I'm stupid, so I still went ahead with it). To replace the gear between the worm and cam gear, the metal piece covering part of it has to at least be lifted a bit (it's held on by gears on the other side of the mechanism, so it's difficult to remove it completely). One note here is that you also have to remove the gear that's connected to the capstan motor with a belt (seen best in [13] at the top right) in order to lift the metal piece. This gear is held on by both a screw and a spring. The spring is there to help with putting it back in. If the gear is already at the correct position but the screw is still loose, the spring pulls it so the belt is at the correct tension, after which the screw can be screwed down to fasten it properly. Alignment and Mode Switch ------------------------- All the gears have to be aligned properly. This is explained much more clearly in [1], but I did take a few pictures to show at least some parts. Most of it is just looking for holes that should line up. This is all assuming the fully unloaded position where the threading arms connected to the blue and white gear are fully retracted as shown in [13]. I already showed the alignment of the blue and white gears earlier, so I'll only show the remaining parts now. [24] shows a hole at the right side of the slide gear that should line up with a hole below. [25] shows how a small rectangular mark in the mode switch (the gear with the black cover) should match up with the arrow on the white gear beside it (note that there's also a hole in the white gear that matches up with the hole shown in [24]). Also note that the metal ring holding down the white gear is still missing in [25], don't forget to put that back in. I also cleaned the mode switch, but I didn't take any pictures of it. It isn't particularly difficult to open it, you just have to unscrew the two screws shown in [25] and press the clips in the center to separate the two parts. I always clean it inside with isopropyl alcohol (possibly also with a fiberglass pen if it's very oxidized, although I'm not sure if that's ideal) and then add some dielectric grease (I read that that's the type of grease you're supposed to use, but I have no clue what's actually best). The contacts seen on the outside (at the right in the picture) can also be cleaned a bit. 12voltvids just uses DeoxIT (which I've never used before) to clean both the contacts on the inside and outside, but I really don't know what the ideal method is. At the same place in the mechanism, but on the top side, the gears going to the pinch roller need to be aligned[26]. You can see that each of the shown gears has a hole that aligns with another hole underneath (or above, in the case of the red gear). The gray gear also needs to be aligned properly with the tower gear (the tall gear that guides the pinch roller)[27]. There's a hole in the gray gear that aligns with a hole below, and also an arrow pointing at a mark on the tower gear. In order to see this properly, you need to first remove the cover over the tower gear[28]. [1] mentions that it's a good idea to clean the shaft the pinch roller is attached to and grease it as well as the tower gear. If you're careful, you shouldn't have to fix the alignment here at all, but I accidentally messed it up, so the tape got caught on the pinch roller on eject until I properly aligned everything again. Back on the bottom side of the mechanism, the cam gear has to be aligned[29]. You can see that there's a hole in the cam gear that lines up with a hole in the slide gear underneath. There are also three pins that have to go into the right holes so the cam gear can be pressed down properly, which can be a bit finicky. One of the pins is moved by the black plastic piece to the right of the cam gear (as seen in [13]), which can be helpful to move it a bit while pressing on the cam gear. Note that this plastic piece often has different colors in other VCRs, even if they use the same mechanism (in the SLV-815, it was green). Once everything is aligned, the triangular metal piece can be attached above the cam gear again. Don't forget to put in all the metal rings to hold everything down. Loading Mechanism ----------------- I performed one final repair on the loading motor[30]. There is a small coupling connecting the motor to the worm gear that drives the loading mechanism. It was still working in this case, but there was already a crack in it, so I decided to buy a replacement. Van Eck also makes replacements for this[31]. The side of the mechanism is only held on by a few clips, so it can easily be removed[32]. The big gear there can be removed by first removing the metal ring holding it in place, after which the motor can be unscrewed and the new coupling stuck on[33]. During reassembly, the big gear has to be aligned with two holes in the metal side, one of which also should be aligned with holes in the other parts of the loading mechanism, as shown by the screwdriver in [34]. Conclusion ---------- Once all this was finally done, the VCR worked without any problems. Now I just need to figure out what to do with it because I have plenty of working VCRs already... [0] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/slv-e9.jpg [1] https://youtube.com/watch?v=q-geC1fndSg [2] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/inside.jpg [3] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/power_supply_cover.jpg [4] gopher://lumidify.org/0/phlog/2024-11-24-sony-slv-815.txt [5] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/front_panel.jpg [6] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_mechanism.jpg [7] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_mechanism_removed.jpg [8] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/front_panel_board.jpg [9] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/hidden_screw.jpg [10] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/top_mechanism.jpg [11] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/missing_screw.jpg [12] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/stuck_arm.jpg [13] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/bottom_mechanism.jpg [14] https://youtube.com/watch?v=xxp_MrsiYhI [15] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/original_blue_gear.jpg [16] https://van-eck.net/en/product/sony-left-threading-gear-vhs-slv-xxx-3-736-147-01-373614701-pp-0346/ [17] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/blue_gear.jpg [18] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/blue_gear_on_arm.jpg [19] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/blue_gear_alignment.jpg [20] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/broken_plastic.jpg [21] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/replacement_plastic.jpg [22] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/worm_cam_coupling_old.jpg [23] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/slide_gear_old.jpg [24] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/slide_gear_alignment.jpg [25] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/mode_switch_alignment.jpg [26] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/pinch_roller_alignment.jpg [27] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/tower_gear_alignment.jpg [28] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/tower_gear_cover.jpg [29] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/cam_gear_alignment.jpg [30] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_motor_coupling.jpg [31] https://van-eck.net/en/product/motor-pulley-sony-h-mechanism-sony-slv-attached-to-motor-m904-pp-0342/ [32] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_mechanism_open.jpg [33] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_motor_coupling_replaced.jpg [34] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/loading_mechanism_alignment.jpg [35] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/bottom_cover.jpg [36] gopher://lumidify.org/I/phlog/2024-11-24-sony-slv-e9/bottom_open.jpg